Made the pulleys co-planer, installed the new belt, and now it runs ram rod straight again- Elvis has left the building.
Excellent fix! Hey, if you ever need fine adjustment the packages of shim stock are useful. I've also taken apart steel feeler gages and found the exact thickness I needed.
Those 14" Deltas with cast frames are great. I bought one new over 25 years ago and and used it until I got a new 18" Rikon. I cut many 100's of thick turning blanks from green wood for drying. Loved that saw. (I think mine hand a 3/4hp motor.)
I never had that a problem with the drive pulleys. I did replace the stock belt with a link belt.
Other things I did:
- Added a 6" riser block kit.
- Put it on a moble base with a foot lock.
- Installed a quick tension lever found on the discount table at Woodcraft. Detensioned after every use.
- Tried various guides, liked the phonelic Cool Blocks best.
- Aligned the table and fence properly - extremely important. There's an easy method.
- Replaced the tires once.
- After trying others, I mostly used Lennox 1/2"x3tpi blades. Zero problems cutting 12" thick wood, even osage orange and persimmon. Easily to resharpen.
- Bought a Starrett bandsaw tension gauge to set the tension correctly.
The little tension marks on the back of these saws (and clones) are not useful and cannot be trusted. Tension either too low and too high can be a problem Without a good way to check, the best advice was to set the tension for the next wider blade, e.g., for a 1/2" blade set it to the 3/4" mark.
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After checking with the Starrett, I think those popularized methods to set tension such as the finger pressure bend and flutter test are not accurate. A tension gauge, bought or easily shop made, is the way to be sure. Too much tension can put unneded stress on the saw and cause premature wear. Not enough tension can cause vetical bowing in a thick cut and other problems. Have tension gauge, will travel. After checking other saws, I found that almost everyone used insufficient tension.
After some use, the stock tension block began to warp, a big problem. It was poorly made with weak cast metal. A stronger one from Itura did the trick
Also replaced the tension spring with a stronger spring from Itura.
Following advice from Duginski and Lonnie Bird, I adjusted the upper and lower wheels and made them coplaner under tension. This involved repositioning shim washers on the upper wheel and rechecking the alignment after tensioning. This improved the cut, especially when resawing which was tricky before.
I realize some people don't believe it's important to make the upper and lower wheels perfectly coplanar, but I do.
As an example of the improved resawing, I successfully resawed a long board for a friend that I would never have attempted before all the adjustments. He wanted a 2x12x12' Douglas Fir board resawn into four 1/2" boards of equal thickness. I built a tall fence, installed a new blade, magneticlaly clamped fingerboards to the table, hand-supported the back end, and fed the board slowly three times. He supported the board on the outfeed. The result was four thin 12" wide boards cut so well a very light skip-planing made them perfect down the 12' length. (He wanted to incase in the only post of many in his timber frame house that was not solid douglas fir.)
After building the new shop and installing the new Rikon the Delta sat unused until I traded it for an old accordion. That guy got a a real deal.
JKJ